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煉鋼合金減量化智能控制模型及其應用

鄭瑞軒 包燕平 王仲亮

鄭瑞軒, 包燕平, 王仲亮. 煉鋼合金減量化智能控制模型及其應用[J]. 工程科學學報, 2021, 43(12): 1689-1697. doi: 10.13374/j.issn2095-9389.2021.10.07.004
引用本文: 鄭瑞軒, 包燕平, 王仲亮. 煉鋼合金減量化智能控制模型及其應用[J]. 工程科學學報, 2021, 43(12): 1689-1697. doi: 10.13374/j.issn2095-9389.2021.10.07.004
ZHENG Rui-xuan, BAO Yan-ping, WANG Zhong-liang. Intelligent control model of steelmaking using ferroalloy reduction and its application[J]. Chinese Journal of Engineering, 2021, 43(12): 1689-1697. doi: 10.13374/j.issn2095-9389.2021.10.07.004
Citation: ZHENG Rui-xuan, BAO Yan-ping, WANG Zhong-liang. Intelligent control model of steelmaking using ferroalloy reduction and its application[J]. Chinese Journal of Engineering, 2021, 43(12): 1689-1697. doi: 10.13374/j.issn2095-9389.2021.10.07.004

煉鋼合金減量化智能控制模型及其應用

doi: 10.13374/j.issn2095-9389.2021.10.07.004
基金項目: 國家自然科學基金資助項目(51874021);鋼鐵冶金新技術國家重點實驗室基金資助項目(41620020)
詳細信息
    通訊作者:

    E-mail: baoyp@ustb.edu.cn

  • 中圖分類號: TF741

Intelligent control model of steelmaking using ferroalloy reduction and its application

More Information
  • 摘要: 基于K均值聚類法對轉爐出鋼過程的合金損耗進行了研究,分析了影響合金損耗的關鍵因素,并將其分為3個聚類,得到轉爐出鋼合金損耗最低的工藝模式。在此基礎上,開發了基于PCA-BP神經網絡和混合整數線性規劃的合金減量化智能控制系統,并以某煉鋼廠為例進行了實際應用。通過對模型進行在線運行,驗證了模型的準確性和實用性。使用該模型后,提高了合金化鋼液成分準確度,減少由傳統人工經驗計算配料造成的成本浪費和成分超標等情況,優化了合金配料方案,降低了煉鋼合金化成本,不同鋼種鐵合金加入總成本降低5.95%~14.74%,平均降幅11.72%。

     

  • 圖  1  42CrMo轉爐出鋼工序工藝參數聚類分布圖(3個聚類)(a)及噸鋼硅錳耗量(b)和噸鋼中碳錳鐵耗量(c)

    Figure  1.  Cluster distribution map of process parameters in the 42CrMo converter steel discharge process (3 clusters) (a), silicomanganese consumption per ton of steel (b), and medium carbon ferromanganese consumption per ton of steel (c)

    圖  2  模型計算流程圖

    Figure  2.  Model calculation flowchart

    圖  3  合金減量化智能控制模型主界面

    Figure  3.  Main interface of the intelligent control steelmaking ferroalloy reduction model

    圖  4  合金收得率PCA-BP神經網絡建立流程圖

    Figure  4.  Flowchart of the alloy element yield PCA-BP neural network

    圖  5  PCA-BP神經網絡結構圖

    Figure  5.  Structure diagram of the PCA-BP neural network

    圖  6  合金收得率預測誤差頻率分布

    Figure  6.  Frequency distribution of the alloy yield prediction error

    圖  7  模型計算成本與實際成本對比

    Figure  7.  Comparison of the model calculation alloy cost and the actual alloy cost

    表  1  3聚類爐次占比及錳收得率

    Table  1.   3 Clustering proportion and the manganese yield in each cluster

    ClusterManganese yield/%Proportion /%
    Cluster 188.4623.57
    Cluster286.5620.71
    Cluster387.1155.71
    下載: 導出CSV

    表  2  合金收得率預測結果和實際收得率對比

    Table  2.   Comparison of the actual alloy yield and the forecast alloy yield

    NumberActual alloy yield/%Forecast alloy yield/%Error/%
    194.4095.891.48
    295.6895.65–0.02
    395.0893.83–1.24
    495.8295.05–0.76
    595.8895.960.08
    695.6696.280.62
    796.5195.23–1.27
    897.0795.44–1.62
    下載: 導出CSV

    表  3  工業試驗結果

    Table  3.   Results of the industrial test

    Furnace numberO2 consumption/
    (m3?t–1)
    Tapping
    temperature/℃
    Hot metal
    ratio
    Mn
    yield/%
    Past average
    cost/(¥·t–1)
    Current
    cost/ (¥·t–1)
    Reduce
    costs /(¥·t–1)
    Decrease
    rate /%
    Whether the ingredients are qualified
    Control group52.2016410.9286.52198.4
    156.4615850.7786.60198.4167.530.911.68
    250.4815810.7787.03198.4170.128.311.67
    356.7715890.7889.31198.4175.223.214.24
    453.3715810.7889.37198.4159.938.45.95
    559.4515310.9189.65198.4160.537.99.27
    645.9715820.7889.66198.4166.332.114.03
    746.5415710.7689.80198.4161.836.69.82
    847.6215840.9290.25198.4175.123.39.24
    949.8315830.9290.26198.4168.430.014.74
    1050.8415750.7790.35198.4161.137.312.70
    1151.4815820.7890.58198.4170.827.611.46
    1255.7615710.7890.64198.4161.137.314.06
    1351.3515690.891.10198.4166.531.813.52
    下載: 導出CSV
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  • 收稿日期:  2021-10-07
  • 網絡出版日期:  2021-11-05
  • 刊出日期:  2021-12-24

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